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This paper presents several case histories where ductile iron pipeline sections have been investigated to ascertain the corrosioncontrol benefits of polyethylene encasement. Investigative procedures, included cell-to-cell potential surveys, side-drain technique measurements, in-situ and laboratory soil tests, pipe-to-soil potential measurements and excavation inspections.
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A case study where MIC was recognized as primary cause of failure for an encased ductile iron water pipeline. The cathodically protected pipe was located within the proximity a creek crossing and had suffered from multiple failures.
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Watermain failures are not often recognized as corrosion but are usually referred to merely as “watermain breaks” because watermain pipe appears sound prior to failure. Some of the causes of watermain breaks are poor design, improper installation, surge or water hammer, soil movement, manufacturing defects, impact, internal corrosion, and external corrosion. Figure 1 shows some of the possible causes of the DI pipe.