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Martensitic Stainless Steel (SMSS) is widely used for downhole production tubing and liners in the Oil & Gas industry. Optimization of the tubular material chemistry, cleanliness and manufacturing route has delivered useful performance in H2S-containing environments (specifically SSC and stress corrosion cracking [SCC])3 resistance4,5,6. Some tubular accessories and most completion equipment require sizes not readily delivered by tubular product form. In these instances, bar stock material is a pragmatic choice.
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A 9-5/8 inch (244.8 mm) Tubing Retrievable Safety Valve (TRSV), which is a type of Sub Surface Safety Valve (SSSV) governed by API Specification 14A, was found to have failed when retrieved during workover operations in a gas production well in June 2019. This TRSV was installed in the well in November 2013 and was in production service from 2015 until November 2018 when the well was shut in for maintenance of surface equipment. In March 2019, with the well still shut in for maintenance, a rapid increase in the tubing-casing annulus (TCA) pressure was observed.